Snettisham
2010 - 1: Pimp My Boat
April 10 - May 9

Looking up Taku Inlet (Taku Glacier between the points and
Devil's Paw visible above the ice field)
I
felt like I was just recovering from last summer. It was March
and the late winter sunshine gleaming off the
snow-capped Coast Mountains down
the channel were just starting to look
appealing as I pulled into work some mornings. I started to think
about
boat maintenance and whether it was all worth it. For better or
for
worse, those thoughts were forcibly put on hold while I spent nearly a
month
jet-setting around the continent (New Orleans, Manzanillo (Mexico),
Washington,
D.C.). When I returned in late April, I finally began work,
though operating
more from habit and inertia than enthusiasm.
As for the work, there was much to do. Having plowed
and pounded through a few seasons of ocean fun, the Ronquil had
a bit of
deferred maintenance that I was determined to face. Two days
before I
left for Washington, D.C., I made my annual first trip to Western Auto, quite
pleased that I beat the spring weekend rush, and managed to purchase
everything
on my long, well-prepared list--the way that trip went, I might only
have to
return for bits of hardware here and there! The next day I
tightened down
the port railing with some new hardware (which had partially detached
itself
from the hull). That victory was followed by frustration when I
discovered through some confusion that the latches that hold up the
folding
metal hatch beneath the center window (between the dashboards) were
riveted
on. So were the boards on which the two seats rest. So much
for simply
unscrewing them and replacing the screws! I pried the most
offending
latch off with a screwdriver, breaking it in the process, and pulled up
a few
of the loose rivets on the seat boards before calling it quits.
The
serious work started a few days after I returned from Washington, already the
latter half of April. The first section below describes the boat
maintenance agonies and successes, followed by a quick
report on the
first trip
to Snettisham of the summer.
4/17 - Saturday
One of the main tasks of the spring was to replace the two seats.
The
vinyl on both had long since split, allowing the foam inside to
soak up
copious rain and remain wet through dry periods. More
importantly, the
metal braces holding up the back of the passenger seat had collapsed
late last
summer and no longer offered support. But to do that, I had to
remove the
existing seats, and I knew nothing about boat seats. Somehow the
brackets
on which they were attached were attached to the boards beneath then,
but
how!? There was no way to access the bracket under the seat, so
how could
I unscrew it? It was clear that the whole board needed to come
off.
Which was not as easy as it sounds! Each board had one or two
diagonal
braces holding them down that originate from the side of the
boat. These
were relatively easy to unscrew. The boards themselves sit on
flanges
that flare out from the metal box that supports the seat. The
rivets
that secured the boards to the flanges were quite a bit more difficult
to
remove. I managed to pry many of them out (since several were
loose to
begin with), but some of them were still quite secure. My dad
came down
with an electric drill and showed me how to simply drill the heads off
to pry up the boards, which worked pretty well. Beneath the seat
boards I
found scraps of 1" or so styrofoam that seemed to be collapsing
downward
and not fully filling the space. When I pulled the styrofoam out
I found
at the bottom of each well a 2" piece of solid foam, saturated with
water
and broken into several pieces; there was no bottom to the seat boxes
(i.e.,
they were open to the bilge), so I think these pieces were meant to be
floor
boards that kept the styrofoam out of the bilge, but which had failed
over
time.
I threw the seat boards with their seats attached over the side of the
boat,
then hopped down after them and used a hammer and a couple of crow bars
to
wrench the seats and brackets off. The brackets were screwed in to the
boards,
but I still couldn't figure out how anyone could access the head of the
screw
to screw them in once the seat was attached to them (or, conversely, no
way to
attach the seat once the bracket is screwed into the board). Like
the
brackets (which were actually swivels, of course), the screws were
horribly
rusted. I decided that I also wanted to replace the seat boards,
as they
were chipped and rotten and generally unattractive. In even worse
shape
was the hatch cover in the bow over the anchor compartment, which was
so rotten
that hardware ripped right out of it and I spent most of last summer
without a handle
to lift it up. So I removed its hinges and took it off the
boat.
That day I also pried off the other non-functional latch from the
center hatch.
4/18 - Sunday
At 10:00 am I went up to my parent's house with my three boards to
replace
where my dad had a nice new piece of marine plywood (who knew that such
a thing
existed!?). I traced each board out with a sharpie, struggling to
figure
out where the actual lines should be between the rotten holes in the
edge of
the boards. The lines followed the curves of the boat and were
not
entirely straight. The edges were also beveled, especially in the
bow
piece where it rests against the narrowing hull. I cut the
pieces, then
took them back down the driveway to the boat to see if they fit, a
process I
repeated many times. Each time I came back my dad used his
planer,
grinding the anchor hatch piece down repeatedly until it fit
perfectly.
In the end I had three beautiful boards; I couldn't have done it
without my
dad's help.
That afternoon I decided I'd better go ahead and get my boat to the
welder, and
I figured the sooner the better with all the spring maintenance going
on around
town. One of the horizontal braces that support the main
floorboard had
broken loose entirely, another was half loose, and there were some
other issues
with the aluminum structure. But in order to get to the welder,
I needed
to switch trailers. I'd purchased a new trailer last fall, but
not until
after I'd pulled the boat, so the Ronquil
still sat on its older trailer which
had
failed sufficiently last summer that I was unwilling to drive it
farther that
the harbor. I was nervous about it, so I enlisted Chris's company
to
drive with me to
So we pulled the boat up to the trailer, but the hull scraped against
the bottom
of it--it was clear that it would need to be adjusted so the boat would
ride
higher. We tied the boat back up and pulled the trailer back onto
the
parking lot. This was not unexpected (though I'd had some hope
that it wouldn’t
be necessary) and I'd brought along wrenches and sockets. Chris
and I
managed to raise the skids as high as they would go by moving bolts (it
took a
bit of effort), trying to keep them symmetrical as we went. This
time when we tried it, the
Ronquil scooted right up and
sat squarely and evenly on the
skids.
Perfect. I headed up the ramp, not hearing Chris yelling at me
until I
reached the top and saw him running after the truck. One of the
trailer
wheels
was flat. Half way between the water and the parking lot, I
slowly pulled
into a parking spot ahead and we assessed the situation. Back
home I
thought I had a spare tire from the other trailer, so we unhitched the
boat,
discovering that it was incredibly stern heavy and would have plowed
into the
ground if we didn't hold the bow down. Puzzled, we loaded the bow
with
several log rounds that were lying around to weight it down. Back
at home
we found the spare tire, grabbed my floor jack, and returned. We
jacked
up the trailer, then Chris valiantly took control and removed the
tire. I
put the new tire on, thankful that it fit, and Chris began the process
of
securing it. During this time I kept wondering where the nozzle
to fill
the tire with air might be...unfortunately, I didn't bring this up to
Chris
until after he'd finished the job. Turns out we put the tire on
backwards. No, that's not true. I put the tire on
backwards, the
only thing I'd actually contributed to the job. After some
grumbling, we
decided the best bet was to go ahead and switch it there, so Chris did
the job
over again. We pumped it up with a bicycle pump and headed home,
arriving
three hours after we started. Driving home, I kept looking back
to see
how beautifully the boat was riding, high off the trailer, straight,
and
comfortable. It made me realize how poorly my trailer was fairing
for
years! This made up for some of the frustrations of the
afternoon.
Back at home we found the boat very easy to wheel around with the stern
so
heavy and, once in place, loaded the bow down with rocks to keep it
upright.
4/19 - Monday
It turns out that you can also move the post that the nose of the boat
nudges
up against at the front of the trailer, which allows
you to
adjust the position of the boat depending on its length and weight (I
learned
this from my dad). I came home from lunch on Monday and loosened
the
U-bolts that held the post in place, nudging it forward with a hammer a
little
over a foot, or as far as it would go before it ran into the trailer
lights. I inched the boat forward with the winch until it nearly
nudged
the post again and, presto, I was suddenly unable to pull the stern
down or
lift the bow up with all my strength. I hitched it up and headed
out to
Simpco Welding where I dropped it off with an explanation of the
problem and my
bilge pump so they could also create a mount for the pump and the float
switch. A few weeks earlier I'd assembled all the parts of a
brand new
bilge pump system (scrapping both the old pump and the float switch),
but
hadn't figured out how I'd attach them to the boat.
That night I sanded the three new boards and gave the bottom sides and
edges
their first coat of paint. On Tuesday I put on a second coat of
paint,
then flipped them and painted the tops on Wednesday and Thursday nights.
4/23
- Friday
I knew I wasn't going to make it out on the boat that following
weekend,
but I had hopes that with a weekend of work I might make it out the
next
weekend. On Friday I took an early lunch and picked up the boat,
paying a
ridiculously small fee for the work. Along with the repairs, I
was pleased
to see two handsome, sturdy platforms for the bilge pump system.
At home
I applied new weather-stripping to the center windshield (which swings
open) to
soften the seam and reduce vibrations. It was a lovely sunny
spring day
and I went back to work (the paying kind) in high spirits with the
intent to
leave at 2:30 to continue working on the boat. It turned out to
be a
particularly bad afternoon at work, and I didn't make it out the door
until
four, though I did send all my staff home a little early. That
afternoon I
sanded
down the remaining boards in the bow (which I discovered are also
rotting, but
will last at least another season) and the bench seat toward the stern
of the
boat with my little power sander before putting on a coat of
paint.
Inside I put a final coat of paint on the three new pieces.
4/24 - Saturday
Saturday morning I had a program with the
4/25/10 - Sunday
The next day I was baffled to find that I'd had the two bench seats
backwards
in my mind and what I thought was the top was actually the
bottom. This
was troublesome on two counts: 1) I wanted three coats of paint on the
top of
them (where there were now only two) and 2) I'd been rather sloppy
when
painting the top, allowing more drips to accumulate on the bottom (now
the top)
than I would have otherwise. So, I took them back inside, sanded
down
some of the drips, and put on another coat of paint. Later, I put
them in
place on the boat and marked the holes to be drilled with a
sharpie. Then
I cleaned out the anchor hatch and carefully replaced the line and
spare prop
inside. Looking for something satisfying to finish, I decided to
attach a
latch handle to the new anchor hatch piece, but soon discovered that
the latch
had to be inset into the wood, so I borrowed a chisel from my mother
(all my
tools are at Snettisham), chiseled it out, then took it back inside to
paint
the newly exposed wood (giving it a second coat before bed). I
also
painted a few of the board edges around the bench seat in the back of
the boat
that I'd glossed over before.
That afternoon I headed to Western
Auto and bought a grease gun and hardware to attach the anchor hatch
and the
new bench seats to the boat. I'd never used a grease gun before,
but it
worked perfectly with the first zerk I tried on the kicker. The
next ones
didn't work as well. In the end I determined that I have two
different
zerks on the kicker--why I can't imagine. The manual is very
clear that a
grease gun is the method to use on these fittings, and their location
makes
sense, but they are shaped differently (they have no head to lock the
gun into
place). I consulted both Dru and my dad, but they could offer no
insight;
in the end, I managed to coerce the grease gun into locking into the
two zerks
on the main engine, but not the two remaining pairs on the
kicker. It's
still a mystery.
4/26/10 - Monday
And then it was Monday again. At lunch I came home in the hopes
of
attaching the anchor hatch to the bow. I had an assemblage of
bolts and
screws--some purchased for the occasion, others left from removing them
earlier--and brought out Chris's cordless drill to make holes (mine is
broken). The battery was dead. So was the other
battery.
Thankfully, I'd found both an old electric drill and, in quite a
separate
place, its chuck. After several trips up and down off the bow, I
finally
thought I was ready, and drilled the holes. First I screwed the
hinges to
the bow. Unfortunately, when I screwed the hinges to the hatch I
ran into
the edge of the metal brace that supports it. This forced the
hatch an
eighth or a quarter inch toward the stern...and, consequently, the
hatch no
longer closed unless I stomped on it (not that I would know
that...). I
had similar problems with securing the latch, which I overcame by using
short
screws that were originally on the hinges for the two holes over the
metal
brace (and reused bolts for the other two).
That evening I removed the bolts
from the right hinge and the hatch slid back into place. I
replaced the
screws that had forced the board down with shorter screws that didn't
pass
through the board, but they were too narrow and loose in the holes to
function. Then I replaced the battery case on the stern bench and
put the
battery inside. Inside the house I opened up the big package on
my front
porch--new seats from Tempress! I'd expected to buy seats from
Western
Auto but the only one I liked there did not have a partner and ordering
was two
weeks out. Instead I found a similar chair from the same brand
online
and, though shipping was free, paid extra for expedited shipping (still
hoping
to make it out that weekend). I had elicited the help of an
employee at
Western Auto about securing seats and he'd explained that one could
turn the
swivel so the top and bottom were 90 degrees apart (making sort of an
eight-sided star shape) and then slide bolts into the swivel and
through
pre-drilled holes (after screwing the seat to the swivel). It
made sense,
though the folks that had first secured my seats somehow managed to
screw the
swivels in. In any event, the first thing to do was secure the
swivels to
the seats, which was easily accomplished. I enjoyed sitting on
them on
the living room floor and swiveling around. Finally, I drilled
the holes
for the bolts to secure the bench seats back into place on the boat.
4/27/10 - Tuesday
I headed back to Western Auto at lunch for more hardware. I
bought larger
washers for the bench seats (since it looked like there was room for
them),
bolts and nuts for the seat swivels (checked against in-store swivels
to make
sure they fit), the largest washers I could find to fit those bolts (on
advice
from the guy who talked to me about seats), and wider screws to fit in
the
existing holes for the hinge that might catch better. In
preparation for
securing the bench seats I refilled the wells with foam. To
replace the
bottom pieces that I believe acted as floorboards to prevent the
smaller pieces
from falling into the bilge, I dug out the remaining sheet of hard pink
styrofoam that I'd purchased to insulate my fireplace two winters
ago. I
cut two pieces that fit precisely into the well and functioned
perfectly as
floorboards, then started filling in with the old styrofoam.
Surprisingly, with a few pieces of pink styrofoam through in, the
existing
pieces filled the space fully.
4/28
- Wednesday
The next day at lunch I brought the bench seats and seats with their
swivels
out to the boat to mark where the seats should go. As expected,
this was
a difficult decision. I'd noticed when I took them off that the
two seats
were not positioned symmetrically in either direction. I could
see why
once I started playing with the driver's seats--the wheel is far to the
left of
the console and the seat needs to be far enough forward that the
captain can
comfortably hold the wheel. I weighed these issues against
aesthetics, and came to a compromise that was both attractive and
functional
for both people, leaving plenty of leg room for the passenger.
Marking
the spots was pretty difficult, as the sharpie I had couldn't get at
the right
angle underneath the seat to make obvious marks. I eventually
used a calligraphy
pen, with which I was somewhat more successful, but only in making
faint marks
on at most three of the corners. After work I had a better idea and
made paper
cutouts of the bottom of the swivel, placing them square in relation to
the
edge of the bench seats to match the scrawls I'd made, and tracing them
out. Then I marked holes and drilled them. When I first
placed the
seats and swivels on the benches I panicked for a moment, as there
wasn't enough
room beneath the seat to straighten the bolt enough to drop it down the
hole
(there's less than an inch of room). I quickly realized that the
solution
was to hang the bolts in the swivels before placing them on the boards
and ease
them straight down. With some finagling, I managed to get all
four bolts
down on both swivels. Then came the endless task of tightening
them down,
round and around both seats, tightening and tightening and tightening
until I
was satisfied that they were all secure. They looked great and I
carried
them out to the boat to bolt them down.
First I had to carefully place the
benches down in place, as the bottom of the bolts dug into the
styrofoam and
couldn't slide once they were settled. The holes I'd drilled in
the
boards lined up perfectly with the existing holes in the metal flange,
but were
too small for the bolts I'd purchased, so I couldn't actually put any
of them
in. I'd really thought that this moment would be satisfying after
all the
work I'd put in to replace the boards and seats, but it was all too
frustrating
to enjoy. I couldn't find the right bolts to secure the diagonal
braces,
I couldn't bolt the bench to the flanges, I scratched the paint on the
benches moving the braces around,
one of
the seats got stuck in the folded down position so I couldn't even sit
in it,
etc.
4/29
- Thursday
The next day I started securing the bolts. First I found the
original
bolts for the diagonal braces in the glove compartment of the boat and
quickly
secured those. Then I drilled all the holes in the edge of the bench
wider
until the bolts slid down; somehow I managed to come up two bolts short
for all
the holes (sixteen in all). Then I started securing them, using
larger
washers when I could and smaller ones when they didn't fit. For
some
reason, only about half of the nuts I'd bought worked. They all
looked
identical, but some wound up only half a turn or so and froze, while
the next
would spin all the way up effortlessly. And this was consistent
across
bolts. Thankfully I'd previously purchased a number of nuts of
the same
size and managed to find enough for all but two of the bolts. I
also
found additional bolts that fit the holes and filled those in.
The holes under the front of the seats were inaccessable from above, so
I drilled up through the bottom of the flange and
the bolts
eventually dropped in neatly. In the end, I managed to secure all
bolts
but two, which were missing nuts. Before me was a stack of likely
looking
nuts, none of which worked. I removed the final two bolts to take
with me
to the hardware store to make sure that whatever nut I bought would fit.
4/30 - Friday
I worked hard on Friday and managed to leave work a little after 2:30
after
finishing a number of tasks that needed completion by the end of
April.
On the way home I went by Harri's Plumbing in search of two matching
sliding
latches to replace the ones I'd ripped off the center hatch of the boat
(Western Auto did not have two alike in the size I needed). These
I found
and then went on to the hardware section where I bought screws for the
latches,
screws for the
bilge
pump and float switch (which I'd brought along for
sizing), and nuts for the two final bolts of the benches. It
turns out
that there are, apparently, two sizes of size 10 bolts....or something
like
that. In any event, there were two bins for bolts that fit size
10 bolts
(which is what I had), one of which fit and one of which didn't.
Huh. I bought extras.
At
home I finished bolting in the benches and everything worked
swimmingly, the
seats swiveling grandly. The latches I'd bought were identical to
the old
ones, so they matched the two still on the hatch and the holes lined up
with
the existing holes. Unfortunately, screwing through the thin
metal did
not hold the latches in place. I measured the space behind with
my
leatherman (1"), and went inside to see if I had a 1" board. I
found one that was perfect and marked it to cut. Without a skill
saw in
town, I dug out my jig saw, but had to borrow a blade from my
dad. It
didn't fit, so I used a hand saw instead. Back on the boat with
my little
pieces, I placed them behind the metal that the latches attach to, but
they
weren't tight enough to allow the screws to bite. I had to brace
them
with a screwdriver and use larger screws than the ones I'd purchased
for it. I
wound up using the three extra screws I'd bought to mount the float
switch,
which bear the bulk of the load, using the smaller screws for the other
holes.
On the right side I had to drill larger holes for the bigger screws, in
part to
remove the remnants of rivets. Unfortunately, those two screws
split the
wood, so I wasn't sure it would hold long term. Once the latches
were
secure, I added some weather-stripping to the side of the hatch to
reduce
rattling (cutting off some of its width to fit) and also added a little
piece
of weather-stripping over all the holes in the consoles that the
latches slide
into, drilling holes in them afterwards. All in all it seemed
tight and
secure and rattle-free. I cleaned up the rubble that had built up
on the
boat and brought the entire contents of the glove compartment inside.
5/1 - Saturday
This was the first weekend that the boat would be ready; I'd been
working so
hard for weeks, and yet I couldn't muster any enthusiasm. And so
my plans
were tentative. Saturday morning I decided I wanted to give the
boat a
good scrubbing before launching. Lacking a bilge pump last season
meant
that water often sat in the boat well above the floorboards, leaving an
oily
residue over everything it touched. First I rinsed off the bow
and
anchor, then the cockpit (all of which was non-oily). Then I
started
scrubbing with dish washing detergent. I normally use simple
green, but
it had proven ineffective against this grease; at least the detergent I
was
using was supposed to be biodegradable. I scrubbed the sides of
the boat,
the back of the seat supports, the floorboard, then the walls and floor
of the
well where the gas cans reside. I took out the big gas can and
scrubbed
it, then I scrubbed the underside of the main floorboard. Working
in the
gas well I saw through a hole cut in the back that there was a lot of
sand and
such sitting in the bilge; I tried to take up the floorboard there, but
one of
the screws was buried deep and too stripped to grab, so instead I
repeatedly
sprayed the hose at pressure down the hole in various directions until
the
water eventually ran relatively clear. There was a lot of crud
sitting
down there! Between flushings I scrubbed the shelf on the back of
the
boat where the engines mount.
By
the time I was through it was around noon and I found myself completely
unmotivated to go out. Inside I put some of the emergency kit
items in
fresh ziplocs and brought a few things out to the boat and decided to
try the
next day.
5/2
- Sunday
Having not gone out the day before, I was obligated to try on
Sunday. It
seemed like everyone else had already been out a bunch of times,
fishing and
crabbing, and I was stuck doing maintenance. Perhaps I'd worn
myself out
getting the boat ready, but I still wasn't really in the mood.
After
walking Nigel I did a final bit of cleaning, swabbing out the
compartment under
the bow below the center hatch and the glove compartment. I
hooked the
boat up to my truck, then hooked up the gas line to the gas tank, which
was
about half full. I pumped the siphon, felt it get a little hard,
and I
hooked the garden hose up to the engine to gave it a try. No
luck.
So I pumped some more....and pumped and pumped and pumped and pumped,
but never
felt the gas go anywhere. I took a shower, then drove
Chris's
car to the gas station and bought another five gallons of gas in case
having a
full tank would help. It didn't. Just to check, I unscrewed
the
fuel filter and discovered that a tiny bit of gas was making it
through, even
to the engine, but apparently not enough. I unhooked the hose
from the
gas tank, and a metal ball fell out along with a washer and a spring,
and part
of the plastic mount remained on the gas tank. There would be no
boating
that day.
I
found the spare siphon and hose in the garage, cleaned it, and took it
outside,
but
decided I'd be better off buying a spare fitting and attaching it to
the
existing hose rather than changing the whole line.
5/3
- Monday
The next day I tried to find a spare fitting at Harri's Plumbing, but
none of
them seemed quite right. I went to Western Auto where I bought
two
fittings that looked identical to the one I had. Unfortunately,
they
turned out to be for a different sized hose. I went back and
talked to an
employee, and he showed me which one to buy. It seemed likely
enough--it
was the right make (Yamaha) and it was for the only other hose size,
but the
fitting looked different and I was dubious. He assured me it
would work,
so I went home. By that time I'd removed the gas line fitting
from the
engine, which fell apart in exactly the same way as the other end, so I
bought
two. With a little hot water to loosen up the hose, replacing the
fittings was easy. Getting them to fit the tank and engine was
another
story. After some struggling I eventually forced the new fitting
onto the
gas tank securely. The engine was a little more trouble and I
could not
for the life of me get it on, try as I might. My mother came down
to feed
the hawks and caught me in despair. Couldn't anything just go
right?!
She
and I worked at it for more than an hour, and eventually got it to
fit.
We removed the engine cover to get a better handle on the engine side
of the
fitting and eventually wound up taking the whole flitting out, even
removing
the gas line from the inside of the engine to pull it all the way
out. I
learned a lot about that system. It was unbelievably stubborn,
but we
eventually got it to stick and put everything back together. I
plan to
never touch that fitting again unless I have to! Thanks to my
mother for
helping me through that--I certainly could not have done it without
her.
This time the siphon worked wonders and the boat started right
up. Before working on the fuel line I'd also been struggling to
screw holes in the mounts for the bilge pump system, but was not able
to drill through the thick aluminum supports. She brought down a
much sturdier drill and the bit went right through. Both pump and
float switch mounted easily and we talked about how to attach the wires
so they had the least chance of getting wet. I'd carefully
spliced them, wrapped them in electrical tape, and doused them in
several layers of liquid tape, but the less exposure the better!
5/4
- Tuesday
The next day I put the finishing touches on the boat, securing the
bilge pump wires to the top of the pump with duct tape, running them to
the battery, and hooking them up. I
finished refitting the emergency kit and otherwise loading the boat
with
summer essentials. I was quite pleased with how neat and smart it
looked,
and how much room I had in the glove compartment. I'd thought to
take it
out for a shake down trip after work one day that week, but that never
worked
out and, because summer was getting on, I decided to take the plunge
and head
to Snettisham for an overnight that weekend.
5/8 - Back to the
I'd promised to show Rob a sea lion haulout this spring, so invited him
along
with Chris and I to the homestead for the night. Chris and I got
to
harbor at noon and launched the boat without incident. While I
was
parking the trailer, Rob showed up and we quickly finished loading the
boat and
were ready to go. I lowered the engine, pumped the siphon until
it was
firm, and turned the key. The engine chugged a couple of times,
then
stopped. I tried again. Nothing. The battery was
dead. Just
to be sure, I tightened the battery connections, but to no avail.
I have
to admit that I was a little proud of myself for not breaking down
right there
at the harbor in front of everyone. I was calm, assessing the
situation,
trying to determine if there was a way to solve it or whether I should
bag the
whole weekend. Charging the battery would be time consuming and a
bit of
trouble. I wonder if you can jump boat batteries? I
wondered. So, I
walked up to a guy who was pulling the boat he'd just driven around me
(and who
couldn't have been unaware of my troubles) and asked him if he'd ever
jumped a
boat. He said yes, but suggested that I should try getting a jump
from
the folks who were just then launching the boat (as he was on his way
out). So I shamelessly said hello to the lady who was handling
the lines
on a boat being launched and asked if she could by any chance give me a
jump. She told me to talk to her
husband
at the truck, so I boldly asked
him if he minded giving me a jump. He agreed, so I ran up to the
truck to
get my jumper cables, regretting that Nigel was following me with his
gimpy
leg. The other boat was launching on the other side of the dock,
so we
handed the Ronquil around
and out to the outside of the other
boat. I
tied her on and we tried to see if the cables would reach. They
were a
bit short, so we pulled the Ronquil up a little farther, tied
her off
again, then I clamped the cables onto my battery and he did the same
inside his
cabin. Heart pounding, I turned the key and the engine started
without a
hitch. I thanked them profusely, told them that they were my
heroes, and
pushed off. Sometimes the engine dies when first put in gear,
especially
if it's not warmed up, so I drifted around for several minutes making
sure that
the engine didn't stop. Eventually I lowered the choke lever and
put her
in gear with no trouble, idling back to the dock. We quickly got
the dog
on board and took off, leaving-the-harbor beers in hand. Phew!
Chris enjoyed the new swivels seat
as we headed south and Rob sat on the cooler in the back. It was
a
beautiful afternoon with a light westerly at our stern. A whale
blew
south of
To celebrate the homestead homecoming and a successful shake down
trip/overwintering, we three sat in the sunshine on the deck (newly
swept by
Chris) and shared a bottle of champagne and a snack. Afterwards,
we
thought a fire sounded nice, so Rob set about gathering wood and
getting a
campfire going in the fire pit by the benches while Chris and I
installed the
stove pipe for the wood stove inside. I'd wanted to replace the
horizontal stack with the insulated one that my parents gave me, but it
didn't fit through the wall thimble, so we stuck to the original
pieces. Once we were done, Rob had a fire going, so we gathered
around. Rob impressibly drank a beer that had overwintered
in the
creek (we determined it was an Alaskan IPA from the cap). I
turned on the
propane and lit the pilots on the stove, then made dinner for everyone
which we
ate around the campfire. When we ran out of ready firewood, we
went
inside, lit a fire, and played gin rummy in the light of the new
propane lamps
that Chris and I installed last fall. They worked beautifully.
![]() Leaving the harbor shot |
![]() Rob and Chris on the way |
![]() Sea lions |
![]() Putting the "lion" in "sea lion" (check out that guy in back!) |
![]() Frolicking lion |
![]() Smooch |
![]() Celebrating on the deck |
![]() Photo shoot |
![]() Pollen smoke |
The next morning I wanted to fix the
leak in the water system, so hiked to the top and shut the water off
(or so I
thought). I left the tap running to help drain it out, but it
seemed to
just keep coming. I finally unscrewed the first filter housing,
but water
continued to gush. I finally sent Rob up to check on it, who
discovered
new bear holes near the valve and guessed that a bear may have bumped
the valve
partially open (but I think it was my mistake). The holes are too
close
to the valve to simply cut out the bad section and splice the line, so
the pipe
had to be removed from the valve coupling. I made a feeble
attempt to
slice it off lengthwise, but quickly gave up, realizing that it would
take
considerably more time than I had.
In
the meantime I'd spotted some
interesting ducks at the water's edge just downriver and slowly hiked
over to
check them out. The stunning green and bronze head of the male
gave him
away as a green-winged teal, hanging out with three ladies or immature
males.
While spying on them I heard some rustling in the brush behind me and
was
delighted to see a black porcupine ambling along, stopping behind me to
eat
salmonberry leaves (see photo to right). When I took a step he
spooked and took off at
surprising speed and I discovered that the wary ducks had also fled
when I turned my back. A little later we heard some rustling near
the
lodge
and tried to track it down and Rob eventually spied the porcupine
climbing the
near-vertical forest floor behind the lodge. Having skipped a
formal
breakfast, we ate an early lunch of quesadillas on the deck and watched
a whale
in the inlet, occasionally lunging. Later we watched a beaver
swim by
headed up river. After lunch we outfitted a kayak with a lawn
chair,
rifle, hydrophone, and bow saw for Chris's annual mother's day photo
and went
out on the water for the shoot.
![]() View from the deck |